Many systems require that the primary source of DC power
be converted to other voltages. Battery driven circuitry is
an obvious candidate. The 6V or 12V cell in a laptop computer must be converted to different potentials needed for
memory, disc drives, display and operating logic. In theory,
AC line powered systems should not need DC/DC converters
because the implied power transformer can be equipped
with multiple secondaries. In practice, economics, noise
requirements, supply bus distribution problems and other
constraints often make DC/DC conversion preferable. A
common example is logic dominated, 5V powered systems
utilizing ±15V driven analog components.
The range of applications for DC/DC converters is large,
with many variations. Interest in converters is commensurately quite high. Increased use of single supply powered
systems, stiffening performance requirements and battery
operation have increased converter usage.
Historically, effi ciency and size have received heavy emphasis. In fact, these parameters can be signifi cant, but
often are of secondary importance. A possible reason
behind the continued and overwhelming attention to size
and effi ciency in converters proves surprising. Simply
put, these parameters are (within limits) relatively easy to achieve! Size and effi ciency advantages have their place,
but other system-oriented problems also need treatment.
Low quiescent current, wide ranges of allowable inputs,
substantial reductions in wideband output noise and cost
effectiveness are important issues. One very important
converter class, the 5V to ±15V type, stresses size and
effi ciency with little emphasis towards parameters such
as output noise. This is particularly signifi cant because
wideband output noise is a frequently encountered problem
with this type of converter. In the best case, the output noise
mandates careful board layout and grounding schemes.
In the worst case, the noise precludes analog circuitry
from achieving desired performance levels (for further
discussion see Appendix A, “The 5V to ±15V Converter
— A Special Case”). The 5V to ±15V DC/DC conversion
requirement is ubiquitous, and presents a good starting
point for a study of DC/DC converters.
5V TO ±15V CONVERTER CIRCUITS
Low Noise 5V to ±15V Converter
Figure 1’s design supplies a ±15V output from a 5V input.
Wideband output noise measures 200 microvolts peakto-peak, a 100× reduction over typical designs. Effi ciency
at 250mA output is 60%, about 5% to 10% lower than
conventional types. The circuit achieves its low noise
performance by minimizing high speed harmonic content
in the power switching stage. This forces the effi ciency
trade-off noted, but the penalty is small compared to the
benefi t.
The 74C14 based 30kHz oscillator is divided into a 15kHz
2-phase clock by the 74C74 fl ip-fl op. The 74C02 gates and
10k-0.001μF delays condition this 2-phase clock into nonoverlapping, 2-phase drive at the emitters of Q1 and Q2
(Figure 2, Traces A and B, respectively). These transistors
provide level shifting to drive emitter followers Q3-Q4. The
Q3-Q4 emitters see 100Ω-0.003μF fi lters, slowing drive
to output MOSFETs Q5-Q6. The fi lter’s effects appear at
the gates of Q5 and Q6 (Traces C and D, respectively). Q5
and Q6 are source followers, instead of the conventional
common source connection. This limits transformer rise
time to the gate terminals fi ltered slew rate, resulting in
L, LT, LTC, LTM, Linear Technology and the Linear logo are registered
trademarks of Linear Technology Corporation. All other trademarks are the
property of their respective owners.
an32f
AN29-1
Application Note 29
0.001
CLK-NON
OVERLAP
GENERATOR
22k
74C14
74C02
74C14
74C14
CK
74C02
15kHz, 5μs
NON-OVERLAP
+V
74C74
Q
10k
10k
74C14
74C14
K1
Q1
LEVEL SHIFTS
K2
Q2
Q
D
0.001
0.001
100Ω
150k1k
10k
100Ω
10k
+
POINT
“A”
(SEE TEXT)
BOOST
OUTPUT
≈17V
DC
DIRVERS-
EDGE
SHAPING
Q4
100
1k150k
1N5817
+
2
8
–4V
+
10
+
D1
1N5817
DC
22μF
Q5
1N5817
47
4
5V
D
6
S
1
7
2
8
39
L1
OUTPUT
S
Q6
D
5V
= ±15 COMMON
= +5 GROUND
* = 1% FILM RESISTOR
FET = MTP3055E-MOTOROLA
PNP = 2N3906
NPN = 2N3904
L1 = PULSE ENGINEERING, INC. #PE-61592
= FERRITE BEAD, FERRONICS #21-110J
D3
1N5817
D2
1N5817
TURBO BURST
470
0.001
100μF
+
5V
IN
(4.5V TO 5.5V)
MUR 120
(ALL)
10μF
1μF
+
+15
OUT
OUT
COMMON
–15
OUT
LT1086
+
100μF
+
10μF
LT337A
10μF
+
124*
1.37k*
249*
2.74k*
AN29 F01
+
100
3
LT1054
5
BOOST
Q3
100
0.003
0.003
Figure 1. Low Noise 5V to ±15V Converter
A = 20V/DIV
B = 20V/DIV
C = 20V/DIV
D = 20V/DIV
E = 10V/DIV
F = 10V/DIV
HORIZ = 20μs/DIV
AN29 F02
Figure 2. 5V to ±15V Low Noise Converter Waveforms
well controlled waveforms at the sources of Q5 and Q6
(Traces E and F, respectively). L1 sees complimentary,
slew limited drive, eliminating the high speed harmonics
normally associated with this type converter. L1’s output
is rectifi ed, fi ltered and regulated to obtain the fi nal out-
put. The 470Ω-0.001μF damper in L1’s output maintains
loading during switching, aiding low noise performance.
The ferrite beads in the gate leads eliminate parasitic RF
oscillations associated with follower confi gurations.
The source follower confi guration eases controlling L1’s
edge rise times, but complicates gate biasing. Special
provisions are required to get the MOSFETs fully turned
on and off. Source follower connected Q5 and Q6 require
voltage overdrive at the gates to saturate. The 5V primary
supply cannot provide the specifi ed 10V gate — channel
bias required for saturation. Similarly, the gates must be
pulled well below ground to turn the MOSFETs off. This
is so because L1’s behavior pulls the sources negative
when the devices turn off. Turn-off bias is bootstrapped
from the negative side of Q6’s source waveform. D1 and
the 22μF capacitor produce a –4V potential for Q3 and Q4
to pull down to. Turn-on bias is generated by a 2-stage
an32f
AN29-2
Application Note 29
boost loop. The 5V supply is fed via D3 to the LT®1054
switched capacitor voltage converter (switched capacitor
voltage converters are discussed in Appendix B, “Switched
Capacitor Voltage Converters — How They Work”). The
LT1054 confi guration, set up as a voltage doubler, initially
provides about 9V boost to point “A” at turn-on. When
the converter starts running L1 produces output (“Turbo
Boost” on schematic) at windings 4-6 which is rectifi ed by
D2, raising the LT1054’s input voltage. This further raises
point “A” to the 17V potential noted on the schematic.
These internally generated voltages allow Q5 and Q6 to
receive proper drive, minimizing losses despite their source
follower connection. Figure 3, an AC-coupled trace of the
15V converter output, shows 200μV
noise at full power
P-P
(250mA output). The –15V output shows nearly identical characteristics. Switching artifacts are comparable in
amplitude to the linear regulators noise. Further reduction
in switching based noise is possible by slowing Q5 and
Q6 rise times. This, however, necessitates reducing clock
rate and increasing non-overlap time to maintain available
output power and effi ciency. The arrangement shown
represents a favorable compromise between output noise,
available output power, and effi ciency.
A = 100μV/DIV
(AC-COUPLED)
less than 30μV of output noise. This is almost 7× lower
than the previous circuit and approaches a 1000× improvement over conventional designs. The trade off is effi ciency
and complexity.
A1 is set up as a 16kHz Wein bridge oscillator. The single
power supply requires biasing to prevent A1’s output from
saturating at the ground rail. This bias is established by
returning the undriven end of the Wein network to a DC
potential derived from the LT1009 reference. A1’s output
is a pure sine wave (Figure 5, Trace A) biased off ground.
A1’s gain must be controlled to maintain sine wave output.
A2 does this by comparing A1’s rectifi ed and fi ltered positive output peaks with an LT1009 derived DC reference.
A2’s output, biasing Q1, servo controls A1’s gain. The
0.22μF capacitor frequency compensates the loop, and the
thermally mated diodes minimize errors due to rectifi er
temperature drift. These provisions fi x A1’s AC and DC
output terms against supply and temperature changes.
A1’s output is AC coupled to A3. The 2k –820Ω divider
re-biases the sine wave, centering it inside A3’s input
common mode range even with supply shifts. A3 drives a
power stage, Q2-Q5. The stages common emitter outputs
and biasing permit 1V
at V
= 4.5V. At full converter output loading the
SUPPLY
RMS
(3V
) transformer drive, even
P-P
stage delivers 3 ampere peaks but the waveform is clean
(Trace B), with low distortion (Trace C). The 330μF coupling
capacitor strips DC and L3 sees pure AC. Feedback to A3 is
taken at the Q4-Q5 collectors. The 0.1μF unit at this point
suppresses local oscillations. L3’s secondary RC network
adds additional high frequency damping.
HORIZ = 5μs/DIV
Figure 3. Output Noise of the Low Noise 5V to ±15V Converter.
Appendix H Shows a Modern IC Low Noise Regulator
AN29 F03
Ultralow Noise 5V to ±15V Converter
Residual switching components and regulator noise set
Figure 1’s performance limits. Analog circuitry operating
at the very highest levels of resolution and sensitivity may
require the lowest possible converter noise. Figure 4’s
converter uses sine wave transformer drive to reduce
harmonics to negligible levels. The sine wave transformer
drive combines with special output regulators to produce
Without control of quiescent current the power stage
will encounter thermal runaway and destroy itself. A4
measures DC output current across Q5’s emitter resistor
and servo controls Q6 to fi x quiescent current. A divided
portion of the LT1009 reference sets the servo point at
A4’s negative input and the 0.33μF feedback capacitor
stabilizes the loop.
L3’s rectifi ed and fi ltered outputs are applied to regulators
designed for low noise. A5 and A7 amplify the LT1021’s
fi ltered 10V output up to 15V. A6 and A8 provide the –15V
output. The LT1021 and amplifi ers give better noise performance than three terminal regulators. The Zener-resistor
network clips overvoltages due to start-up transients.
an32f
AN29-3
Application Note 29
OUT
15V
L1
25μH
+
47μF
A7
LT1010
IN
5V
(4.5V TO 5.5V)
4.99k*
A5
–
1/2 LT1013
10k*
22μF
+
L4
100μH
Q4
+
22μF
1N4001
68Ω
AMP
POWER
430Ω
8
+
1μF
MJE2955
50Ω
Q2
OUT
5k
†
330μF
0.1
2N2219
0.1
LT1021
L3
+
OUT
10V
IN
330Ω
534
8
0.1
50Ω
Q3
COMMON
19V
UNREG
*
*
0.005
Q5
MJE3055
2N2905
220μF
+
*
*
1
100Ω
330Ω10k*
1N4001
Q6
0.1Ω
220μF
10k
1k750Ω*
10k*
1N5260B
+
–19V
UNREG
0.22
+
47μF
OUT
–15V
L2
25μH
A8
LT1010
4
A6
–
1/2 LT1013
620Ω
Q
I
LOOP
CONTROL
10k
–
+
A4
1/2 LT1013
0.33
AN29 F04
0.1
+
20k
0.01
LT1006
270Ω
–
1k*
(SELECTED
VALUE—
SEE TEXT)
430Ω
5V
1k
LT1009
2.5
MATED
THERMALLY
200k
–
0.22
2k
Q1
1/2 LT1013
A2
+
OSCILLATOR
10k
STAB. LOOP
3.1k
= 1N4148
= 1N4934
L1, L2 = PULSE ENGINEERING, INC. #PE-92100
L3 = PULSE ENGINEERING, INC. #PE-65064
*
L4 = PULSE ENGINEERING, INC. #PE-92108
= THF337K006P1G
UNMARKED NPN = 2N3904
* = 1% METAL FILM RESISTOR
†
= +5 GROUND
= ±15 COMMON
Figure 4. Ultralow Noise Sine Wave Drive 5V to ±15V Converter
an32f
220Ω
8
A3
+
820Ω
2k
5V
1μF
+
10k
A1
LT1006
47μF
0.22
680Ω
–
220Ω
0.01
8
+
1k
16kHz
OSCILLATOR
1k
+
1k
AN29-4
A = 2V/DIV
B = 2V/DIV
C = 1% DISTORTION
D = 20μV/DIV
HORIZ = 50μs/DIV
Figure 5. Waveforms for the Sine Wave Driven Converter.
Note that Output Noise (Trace D) is Only 30μV
AN29 F05
P-P
L1 and L2 combine with their respective output capacitors to aid low noise characteristics. These inductors are
outside the feedback loop, but their low copper resistance
does not signifi cantly degrade regulation. Trace D, the 15V
output at full load, shows less than 30μV (2ppm) of noise.
The most signifi cant trade-off in this design is effi ciency.
The sine wave transformer drive forces substantial power
loss. At full output (75mA), effi ciency is only 30%.
Before use, the circuit should be trimmed for lowest
distortion (typically 1%) in the sine wave delivered to
L3. This trim is made by selecting the indicated value at
A1’s negative input. The 270Ω value shown is nominal,
with a typical variance of ±25%. The sine wave’s 16kHz
frequency is a compromise between the op amps available gain bandwidth, magnetics size, audible noise, and
minimization of wideband harmonics.
Single Inductor 5V to ±15V Converter
Simplicity and economy are another dimension in 5V to
±15V conversion. The transformer in these converters is
usually the most expensive component. Figure 6’s unusual
drive scheme allows a single, 2-terminal inductor to replace
the usual transformer at signifi cant cost savings. Tradeoffs include loss of galvanic isolation between input and
output and lower power output. Additionally, the regulation
technique employed causes about 50mV of clock related
output ripple.
The circuit functions by periodically and alternately allowing
each end of the inductor to fl yback. The resultant positive
and negative peaks are rectifi ed and fi ltered. Regulation
is obtained by controlling the number of fl yback events
during the respective output’s fl yback interval.
Application Note 29
The leftmost logic inverter produces a 20kHz clock (Trace A,
Figure 7) which feeds a logic network composed of additional inverters, diodes and the 74C90 decade counter. The
counter output (Trace B) combines with the logic network
to present alternately phased clock bursts (Traces C andD)
to the base resistors of Q1 and Q2. When φ1 (Trace B)
is unclocked it resides in its high state, biasing Q2 and
Q4 on. Q4’s collector effectively grounds the “bottom” of
L1 (TraceH). During this interval φ2 (Trace A) puts clock
bursts into Q1’s base resistor. If the –15V output is too
low servo comparator C1A’s output (Trace E) is high, and
Q1’s base can receive pulsed bias. If the converse is true
the comparator will be low, and the bias gated away via
Q1’s base diode. When Q1 is able to bias, Q3 switches,
resulting in negative going fl yback events at the “top” of
L1 (Trace G). These events are rectifi ed and fi ltered to
produce the –15V output. C1A regulates by controlling
the number of clock pulses that switch the Q1-Q3 pair.
The LT1004 serves as a reference. Trace J, the AC-coupled
–15V output, shows the effect of C1A’s regulating action.
The output stays within a small error window set by C1A’s
switched control loop. As input voltage and loading conditions change C1A adjusts the number of clock pulses
allowed to bias Q1-Q3, maintaining loop control.
When the φ1 and φ2 signals reverse state the operating
sequence reverses. Q3’s collector (Trace G) is pulled high
with Q2-Q4 switching controlled by C1B’s servo action.
Operating waveforms are similar to the previous case.
Trace F is C1B’s output, Trace H is Q4’s collector (L1’s “bottom”) and Trace I is the AC-coupled 15V output. Although
the two regulating loops share the same inductor they
operate independently, and asymmetrical output loading is
not deleterious. The inductor sees irregularly spaced shots
of current (Trace K), but is unaffected by its multiplexed
operation. Clamp diodes prevent reverse biasing of Q3
and Q4 during transient conditions. The circuit provides
±25mA of regulated power at 60% effi ciency.
Low Quiescent Current 5V to ±15V Converter
A fi nal area in 5V to ±15V converter design is reduction
of quiescent current. Typical units pull 100mA to 150mA
of quiescent current, unacceptable in many low power
systems.
an32f
AN29-5
Application Note 29
150k*
12.4k*
HP5082-2810
32k
1000pF
5
74C90
÷10
12
= 1N4148
* = 1% METAL FILM RESISTOR
= 74C14
+
1/2 LT1018
–
10k
C1A
10k
10k
5V
300Ω
10k
100Ω
K2
4.7k
K1
4.7k
5V
300Ω
C1B
1/2 LT1018
Q1
2N3906
5V
Q2
2N3904
100Ω
+
–
1k
LT1004
1.2V
5V
2k
Q3
2N5023
–15V
15V
137k*
12.4k*
AN29 F06
OUT
OUT
+
100
L1
145μH
+
Q4
2N3507
2k
5V
100
L1 = PULSE ENGINEERING, INC. # PE-92105
Figure 6. Single Inductor 5V to ±15V Regulated Converter
A = 5V/DIV
B = 5V/DIV
C = 10V/DIV
D = 10V/DIV
E = 10V/DIV
F = 10V/DIV
G = 20V/DIV
H = 20V/DIV
I = 0.05V/DIV (AC-COUPLED)
J = 0.05V/DIV (AC-COUPLED)
K = 1A/DIV
HORIZ = 100μs/DIV
Figure 7. Waveforms for the Single Inductor, Dual-Output,
Regulated Converter
AN29 F07
Figure 8’s design supplies ±15V outputs at 100mA while
consuming only 10mA quiescent current. The LT1070
switching regulator (for a complete description of this
device, see Appendix C, “Physiology of the LT1070”) drives
L1 in fl yback mode. A damper network clamps excessive
fl yback voltages. Flyback events at L1’s secondary are
half-wave rectifi ed and fi ltered, producing positive and
negative outputs across the 47μF capacitors. The positive
16V output is regulated by a simple loop. Comparator
C1A balances a sample of the positive output with a 2.5V
reference obtained from the LT1020. When the 16V output (Trace A, Figure 9) is too low, C1A switches (TraceB)
high, turning off the 4N46 opto-isolator. Q1 goes off, and
the LT1070’s control pin (V
causes full duty cycle 40kHz switching at the V
) pulls high (Trace C). This
C
pin
SW
(Trace D). The resultant energy into L1 forces the 16V
output to ramp quickly positive, turning off C1A’s output.
an32f
AN29-6
5V
IN
(4.5V TO 5.5V)
Application Note 29
16V PRE-REG
0.47
V
GND
10k
19
37
SW
1.2k
2W
MUR120
V
IN
NC
2N3906
LT1070FB
V
C
Q1
L1 = PULSE ENGINEERING, INC. # PE-61592
* = 1% FILM RESISTOR
= +5 GROUND
= ±15 COMMON
1N4148
L1
+
8
+
1N4148
5V
4N46
390k
47μF
47μF
1.2M*
82k
216k*
–
C1A
1/2 LT1017
+
20M
10k
–16V UNREG
10k
0.002
UPDATE
Burst Mode regulators
can achieve lower I
Figure 8. Low I
, Isolated 5V to ±15V Converter
Q
Q
9
3
V
GND
–1N
5
COMP
PNP
0.001μF
3M*500k* 100k
470k
IN
LT1070
2.5V
+IN
REF OUT
74 6
Q2
VN2222
OPTIONAL
(SEE TEXT)
28
OUT
11
FB
COMP
NPN
–16V UNREG
–15V
15V
OUT
2.5M*
0.001μF
100mA
+
500k*
10μF
+
10μF
–15V
OUT
100mA
TO
REF OUT
470k
3.2M
1.5M
–
1/2 LT1017
+
47k
C1B
TO
TO
TO 16V
PRE-REG
1.5k
5.6M
AN29 F08
A = 100mV/DIV
(AC-COUPLED ON
LEVEL)
16V
DC
B = 20V/DIV
C = 2V/DIV
D = 20V/DIV
HORIZ = 5ms/DIV
AN29 F09
Figure 9. Waveforms for the Low IQ 5V to ±15V Converter
The 20M value combined with the 4N46’s slow response
(note the delay between C1A going high and the V
pin
C
rise) gives about 40mV of hysteresis. The LT1070’s onoff duty cycle is load dependent, saving signifi cant power
when the converter is lightly loaded. This characteristic
is largely responsible for the 10mA quiescent current.
The opto-isolator preserves the converters input-output
isolation. The LT1020, a low quiescent current regulator
with low dropout, further regulates the 16V line, giving
the 15V output. The linear regulation eliminates the 40mV
ripple and improves transient response. The –16V output
tends to follow the regulated –16V line, but regulation
is poor. The LT1020’s auxiliary onboard comparator is
compensated to function as an op amp by the RC damper
at Pin 5. This amplifi er linearly regulates the –16V line.
MOSFET Q2 provides low dropout current boost, sourcing
the –15V output. The –15V output is stabilized with the
op amp by comparing it with the 2.5V reference via the
500k-3M current summing resistors. 1000pF capacitors
frequency compensate each regulating loop. This converter
functions well, providing ±15V outputs at 100mA with
only 10mA quiescent current. Figure 10 plots effi ciency
versus a conventional design over a range of loads. For
high loads results are comparable, but the low quiescent
circuit is superior at lower current.
A possible problem with this circuit is related to the poor
regulation of the –16V line. If the positive output is lightly
loaded L1’s magnetic fl ux is low. Heavy negative output
loading under this condition results in the –16V line falling
below its output regulators dropout value. Specifi cally, with
no load on the 15V output only 20mA is available from
the –15V output. The full 100mA is only available from
an32f
AN29-7
Application Note 29
100
90
80
70
60
50
40
EFFICIENCY (%)
30
20
10
0
0
LOW QUIESCENT
CURRENT DESIGN
CONVENTIONAL
DESIGN
2010
4030
50
OUTPUT CURRENT (mA)
60 7090
80
100
AN29 F10
Figure 10. Effi ciency vs Load for the Low IQ Converter
the –15V output when the 15V output is supplying more
than 8mA. This restriction is often acceptable, but some
situations may not tolerate it. The optional connection in
Figure 8 (shown in dashed lines) corrects the diffi culty.
C1B detects the onset of –16V line decay. When this occurs its output pulls low, loading the 16V line to correct
the problem. The biasing values given permit correction
before the negative linear regulator drops out.
MICROPOWER QUIESCENT CURRENT CONVERTERS
Many battery-powered applications require very wide
ranges of power supply output current. Normal conditions
require currents in the ampere range, while standby or
“sleep” modes draw only microamperes. A typical laptop
computer may draw 1 to 2 amperes running while needing only a few hundred microamps for memory when
turned off. In theory, any DC/DC converter designed
for loop stability under no-load conditions will work. In
practice, a converter’s relatively large quiescent current
may cause unacceptable battery drain during low output
current intervals.
Figure 11 shows a typical fl yback based converter. In this
case the 6V battery is converted to a 12V output by the
inductive fl yback voltage produced each time the LT1070’s
pin is internally switched to ground (for commentary
V
SW
on inductor selection in fl yback converters see Appendix D,
“Inductor Selection for Flyback Converters”). An internal
40kHz clock produces a fl yback event every 25μs. The
energy in this event is controlled by the IC’s internal error amplifi er, which acts to force the feedback (FB) pin to
a 1.23V reference. The error amplifi ers high impedance
output (the VC pin) uses an RC damper for stable loop
compensation.
This circuit works well but pulls 9mA of quiescent current.
If battery capacity is limited by size or weight this may be
too high. How can this fi gure be reduced while retaining
high current performance?
V
IN
L1*
6V
50μH
V
IN
LT1070
GNDV
+
MUR8100
V
SW
FB
C
1k
1μF
+
470μF
*PULSE ENGINEERING, INC
#PE-51515
10.7k
1.24k
AN29 F11
V
12V
OUT
Figure 11. 6V to 12V, 2 Amp Converter with 9mA Quiescent Current
A solution is suggested by considering an auxiliary V
function. If the V
pin is pulled within 150mV of ground the
C
pin
C
IC shuts down, pulling only 50 microamperes. Figure 12’s
special loop exploits this feature, reducing quiescent current to only 150 microamperes. The technique shown is
particularly signifi cant, with broad implication in battery
powered systems. It is easily applied to a wide variety of
DC/DC converters, meeting an acknowledged need across
a wide spectrum of applications.
Figure 12’s signal fl ow is similar to Figure 11, but additional
circuitry appears between the feedback divider and the V
C
pin. The LT1070’s internal feedback amplifi er and reference
are not used. Figure 13 shows operating waveforms under
no-load conditions. The 12V output (Trace A) ramps down
over a period of seconds. During this time comparator
A1’s output (Trace B) is low, as are the 74C04 paralleled
inverters. This pulls the V
IC in its 50μA shutdown mode. The V
pin (Trace C) low, putting the
C
pin (Trace D) is
SW
high, and no inductor current fl ows. When the 12V output
drops about 20mV, A1 triggers and the inverters go high,
pulling the V
pin pulses the inductor at the 40kHz clock rate, caus-
V
SW
pin up and turning on the regulator. The
C
ing the output to abruptly rise. This action trips A1 low,
forcing the V
pin back into shutdown. This “bang-bang”
C
control loop keeps the 12V output within the 20mV ramp
an32f
AN29-8
+
6V
IN
(4.5V TO 8V)
47μF
L1
50μH
V
SW
LT1070
V
GND
C
R6
200Ω
+
C2
47μF
MUR405
FBNC
3.6M*
Application Note 29
–
A2
1/2 LT1017
+
1.2M*
+
C1
2700μF
6V
A1
1/2 LT1017
–
+
“LOW BATT”
R3
2M
12V
R1
1M*R7100k
R2
120k*
OUT
C3
1500pF
UPDATE
Micropower regulators using
Burst Mode operation are available
10pF**
** = OPTIONAL. SEE TEXT
= 1N4148
* = 1% METAL FILM RESISTOR
= 74C04
L1 = PULSE ENGINEERING, INC. # PE-51515
Figure 12. 6V to 12V, 2 Amp Converter with 150μA Quiescent Current
hysteresis window set by R3-R4. Diode clamps prevent
pin overdrive. Note that the loop oscillation period of
V
C
4 to 5 seconds means the R6-C2 time constant at V
C
is
not a signifi cant term. Because the LT1070 spends almost
all of the time in shutdown, very little quiescent current
(150μA) is drawn.
Figure 14 shows the same waveforms with the load increased to 3mA. Loop oscillation frequency increases to
keep up with the loads sink current demand. Now, the V
C
pin waveform (Trace C) begins to take on a fi ltered appearance. This is due to R6-C2’s 10ms time constant. If
R4
10k
AN29 F12
A = 0.02V/DIV
(AC-COUPLED)
B = 5V/DIV
C = 2V/DIV
D = 10V/DIV
R5
180k
LT1004
1.2V
6V
Figure 13. Low I
HORIZ = 1s/DIV
Converter Waveforms with No Load
Q
(Traces B and D Retouched for Clarity)
AN29 F13
an32f
AN29-9
Application Note 29
the load continues to increase, loop oscillation frequency
will also increase. The R6-C2 time constant, however,
is fi xed. Beyond some frequency, R6-C2 must average
loop oscillations to DC. Figure 15 shows the same circuit
points at 1 ampere loading. Note that the VC pin is at DC,
and repetition rate has increased to the LT1070’s 40kHz
clock frequency. Figure 16 plots what is occurring, with
a pleasant surprise. As output current rises, loop oscillation frequency also rises until about 500Hz. At this point
the R6-C2 time constant fi lters the V
LT1070 transitions into “normal” operation. With the V
pin to DC and the
C
C
pin at DC it is convenient to think of A1 and the inverters as a linear error amplifi er with a closed-loop gain set
by the R1-R2 feedback divider. In fact, A1 is still duty
cycle modulating, but at a rate far above R6-C2’s break
frequency. The phase error contributed by C1 (which was
selected for low loop frequency at low output currents) is
dominated by the R6-C2 roll off and the R7-C3 lead into
A1. The loop is stable and responds linearly for all loads
beyond 80mA. In this high current region the LT1070 is
desirably “fooled” into behaving like Figure 11’s circuit.
A formal stability analysis for this circuit is quite complex,
but some simplifi cations lend insight into loop operation.
At 100μA loading (120kΩ) C1 and the load form a decay
time constant exceeding 300 seconds. This is orders of
magnitude larger than R7-C3, R6-C2, or the LT1070’s
40kHz commutation rate. As a result, C1 dominates the
loop. Wideband A1 sees phase shifted feedback, and very
1
low frequency oscillations similar to Figure 13’s occur
.
Although C1’s decay time constant is long, its charge
time constant is short because the circuit has low sourcing impedance. This accounts for the ramp nature of the
oscillations.
Increased loading reduces the C1 load decay time constant. Figure 16’s plot refl ects this. As loading increases,
the loop oscillates at a higher frequency due to C1’s decreased decay time. When the load impedance becomes
low enough C1’s decay time constant ceases to dominate
the loop. This point is almost entirely determined by R6
and C2. Once R6 and C2 “take over” as the dominant time
constant the loop begins to behave like a linear system.
In this region (e.g. above about 75mA, per Figure 16) the
LT1070 runs continuously at its 40kHz rate. Now, the R7C3 time constant becomes signifi cant, performing as a
2
simple feedback lead
to smooth output response. There is
A = 0.02V/DIV
(AC-COUPLED)
B = 5V/DIV
C = 2V/DIV
D = 10V/DIV
HORIZ = 20ms/DIV
AN29 F14
Figure 14. Low IQ Converter Waveforms at Light Loading
A = 0.02V/DIV
B = 5V/DIV
C = 2V/DIV
D = 10V/DIV
AN29 F15
2.5A
80
100
AN29 F16
Figure 15. Low I
550
500
450
400
350
300
250
IQ = 150μA
200
150
LOOP FREQUENCY (Hz)
100
50
0
0
HORIZ = 20μs/DIV
Converter Waveforms at 1 Amp Loading
Q
LINEAR REGION
EXTENDS TO
0.2Hz
20
OUTPUT (mA)
60
40
Figure 16. Figure 12’s Loop Frequency vs Output Current.
Note Linear Loop Operation Above 80mA
1
Some layouts may require substantial trace area to A1’s inputs. In such
cases the optional 10pF capacitor shown ensures clean transitions at A1’s
output.
2
“Zero Compensation” for all you technosnobs out there.
AN29-10
an32f
A = 10V/DIV
B = 0.1V/DIV
(AC-COUPLED)
HORIZ = 5ms/DIV
Figure 17. Load Transient Response for Figure 12’s
Low IQ Regulator
AN29 F17
Application Note 29
3
constant decay
is visible as Trace B approaches steady state between the
4th and 5th vertical divisions.
A2 functions as a simple low-battery detector, pulling low
when V
drops below 4.8V.
IN
Figure 18 plots effi ciency versus output current. High
power effi ciency is similar to standard converters. Low
power effi ciency is somewhat better, although poor in
the lowest ranges. This is not particularly bothersome,
as power loss is very small.
(“rattling” is perhaps more appropriate)
100
90
80
70
60
50
40
EFFICIENCY (%)
30
20
10
0
0
Figure 18. Effi ciency vs Output Current for Figure 12.
Standby Effi ciency is Poor, But Power Loss Approaches
Battery Self Discharge
TYPICAL OPERATING
15mA
3mA
650μA
IQ = 150μA
0.5
1
OUTPUT CURRENT (A)
REGION
TYPICAL STANDBY
REGION
1.5
2
2.5
AN29 F18
a fundamental trade-off in the selection of the R7-C3 lead
network values. When the converter is running in its linear
region they must dominate the DC hysteresis deliberately
generated by R3-R4. As such, they have been chosen for
the best compromise between output ripple at high load
and loop transient response.
This loop provides a controlled, conditional instability
instead of the more usually desirable (and often elusive)
unconditional stability. This deliberately introduced characteristic lowers converter quiescent current by a factor of
60 without sacrifi cing high power performance. Although
demonstrated in a boost converter, it is readily exportable
to other confi gurations. Figure 19a’s step-down (buck
mode) confi guration uses the same basic loop with almost
no component changes. P-channel MOSFET Q1 is driven
from the LT1072 (a low power version of the LT1070) to
convert 12V to a 5V output. Q2 and Q3 provide current
limiting, while Q4 supplies turn off drive to Q1. the lower
output voltage mandates slightly different hysteresis biasing than Figure 12, accounting for the 1MΩ value at the
comparators positive input. In other respects the loop and
its performance are identical. Figure 19b uses the loop in
a transformer based multi-output converter. Note that the
fl oating secondaries allow a –12V output to be obtained
with a positive voltage regulator.
Low Quiescent Current Micropower 1.5V to 5V
Converter
Despite the complex dynamics transient response is quite
good. Figure 17 shows performance for a step from no
load to 1 ampere. When Trace A goes high a 1 ampere load
appears across the output (Trace B). Initially, the output
sags almost 150mV due to slow loop response time (the
R6-C2 pair delay V
pin response). When the LT1070 comes
C
on (signaled by the 40kHz “fuzz” at the bottom extreme
of Trace B) response is reasonably quick and surprisingly
well behaved considering circuit dynamics. The multi-time
Figure 20 extends our study of low quiescent current converters into the low voltage, micropower domain. In some
circumstances, due to space or reliability considerations, it
is preferable to operate circuitry from a single 1.5V cell. This
eliminates almost all ICs as design candidates. Although
it is possible to design circuitry which runs directly from
®
a single cell (see LTC
Application Note 15, “Circuitry For
Single Cell Operation”) a DC/DC converter permits using
higher voltage ICs. Figure 20’s design converts a single
3
Once again, “multi-pole settling” for those who adore jargon.
an32f
AN29-11
Application Note 29
12V
(8V TO 16V)
IN
0.4Ω
1k100Ω
Q2
2N3906
Q1
IRF-9531
Q4
2N3904
L1
100μH
MUR405
5V
+
2700μF
1M
1M*
OUT
1500pF
100k
+
10μF
2k
1N4148
1N4148
1N4148
L1 = PULSE ENGINEERING, INC. # PE-92108
** = OPTIONAL. SEE TEXT
* = 1% FILM RESISTOR
Q3
2N3904
= 74C04
+
V
IN
V
LT1072
C
200Ω
47μF
V
GND
SW
FBNC
10k
12V
IN
–
1/2 LT1017
+
10pF**
UPDATE
Burst Mode regulators
can achieve lower I
Q
340k*
10k470k
LT1004
1.2V
AN29 F19a
12V
IN
Figure 19a. The Low Quiescent Current Loop Applied to a Buck Converter
1.5V cell to a 5V output with only 125μA quiescent current.
Oscillator C1A’s output is a 2kHz square wave (Trace D,
Figure 21). The confi guration is conventional, except that
the biasing accommodates the narrow common mode
range dictated by the 1.5V supply. To maintain low power,
C1A’s integrating capacitor is small, with only 50mV of
swing. The parallel connected sides of C2 drive L1. When
the 5V output (Trace A) coasts down far enough C1B
goes low (Trace B), pulling both C2 positive inputs close
to ground. C1A’s clock now appears at the paralleled C2
outputs (Trace C), forcing energy into L1. The paralleled
outputs minimize saturation losses. L1’s fl yback pulses,
rectifi ed and stored in the 47μF capacitor, form the circuits
DC output. C1B on-off modulates C2 at whatever duty
cycle is required to maintain the circuits 5V output. The
LT1004 is the reference, with the resistor divider at C1B’s
positive input setting the output voltage. Schottky clamping
of C2’s outputs prevents negative going overdrives due to
parasitic L1 behavior.
AN29-12
an32f
Application Note 29
12V
MUR120
L1
7
+
t
IN
22μF
+
4
t
2
2k
2W
0.2μF
3
8
9
MUR120
10
t
11
MBR360
5
+
+
t
L1
t
1
6
MUR120
V
GND
IN
LT1071
V
SW
V
C
+
FBNC
200Ω
C2
47μF
74C04 (5)
R6
470μF
470μF
C1
2700μF
LT1086
LT1086
1.2k
1.2k
11k
12V
IN
A1
1/2 LT1017
11k
–
+
+
10μF
12V
+
10μF
–12V
V
OUT
5V
1A
R3
R1
1M
1M*R710k
C3
0.005
R2
453k*
1N4148
L1 = PULSE ENGINEERING, INC. # PE-65108
* = 1% FILM RESISTOR
** = OPTIONAL. SEE TEXT
Figure 19b. Multi-Output, Transformer Coupled Low Quiescent Current Converter
The 1.2V LT1004 reference biasing is bootstrapped to the
5V output, permitting circuit operation down to 1.1V. A
10M bleed to supply ensures start-up. The 1M resistors
divide down the 1.2V reference, keeping C1B inside common mode limits. C1B’s positive feedback RC pair sets
about 100mV hysteresis and the 22pF unit suppresses
high frequency oscillation.
The micropower comparators and very low duty cycles at
light load minimize quiescent current. The 125μA fi gure
noted is quite close to the LT1017’s steady-state currents.
As load increases the duty cycle rises to meet the demand,
10pF**
R4
1N4148
10k
LT1004
1.2
AN29 F19b
R5
180k
12V
IN
requiring more battery power. Decrease in battery voltage
produces similar behavior. Figure 22 plots available output
current versus battery voltage. Predictably, the highest
power is available with a fresh cell (e.g., 1.5V to 1.6V),
although regulation is maintained down to 1.15V for 250μA
loading. The plot shows that the test circuit continued to
regulate below this point, but this cannot be relied on in
practice (LT1017 V
= 1.15V). The low supply voltage
MIN
makes saturation and other losses in this circuit diffi cult
to control. As such, effi ciency is about 50%.
an32f
AN29-13
Application Note 29
3.9M
–
1.5M
150pF
3.9M
1.5V
470k
* = 1% METAL FILM RESISTOR
PNP = 2N3906
NPN = 2N3904
L1 = TRIAD # SP-29
C1A
1/2 LT1017
+
2M
240k
1.5V
150k
10M
–
C2B
1/2 LT1017
+
–
C2A
1/2 LT1017
+
V
IN
(1.1V TO 2V)
NC
1N4148
HP5082-2810
HP5082-2810
L1
5
6
HP-5082-2810
+
2.2μF
5V
OUT
22pF
1M*
0.001
+
C1B
1/2 LT1017
–
1M*
10M
360k
10M
V
IN
LT1004
1.2V
34
+
NC
2
1
4.3M*
47μF
619k*
390k
0.001
OPTIONAL FOR
NEGATIVE
OUTPUT
(SEE TEXT)
1.5V
C2B
C2A
Figure 20. 800μA Output 1.5V to 5V Converter
A = 100mV/DIV
(AC-COUPLED ON
LEVEL)
5V
DC
B = 2V/DIV
C = 2V/DIV
D = 2V/DIV
HORIZ = 5ms/DIV
AN29 F21
Figure 21. Waveforms for Low Power 1.5V to 5V Converter
5
6
TO 390kΩ
OF C2B
47μF
+
620k
14
3
850
800
750
= 5V
700
650
OUT
600
550
500
450
400
350
300
250
200
150
100
OUTPUT (μA) AVAILABLE AT V
22pF
1.2M*10k5.1M
50
0
+
–
IQ = 125μA
0
1.05 1.15
C1B
V
OUT
EFFICIENCY ≈ 50%
GUARANTEED MINIMUM
OPERATING VOLTAGE
1.25
INPUT VOLTAGE (V)
10M 47k
= 5V
LT1017
1.35
LT1004
1.2V
1.45
V
1.55
AN29 F22
IN
Figure 22. Output Current Capability vs Input Voltage for Figure 20
AN29 F20
AN29-14
an32f
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