Market Forge PS-3E Service Manual

PS-3E AND PS-6E
ELECTRIC CONVECTON STEAMERS
PARTS AND SERVICE MANUAL
EFFECTIVE AUGUST 1, 2014
The Company reserves the right to make substitution in the event that items specied are not available.
ERRORS: Descriptive and/or typographic errors are subject to correction.
44 Lakeside Avenue, Burlington, Vermont 05401 USA Telephone: (802) 658-6600 Fax: (802) 860-3732
MARKET FORGE INDUSTRIES
www.mi.com
P/N 14-0285 Rev A (8/14)
TABLE OF CONTENTS
SERVICE AND ADJUSTMENTS .........................................................3
WIRING DIAGRAMS ...................................................................4
ILLUSTRATED PARTS LIST ............................................................7
SERVICE AND ADJUSTMENTS
NOTICE
Contact the factory, the factory representa­tive or local service company to perform any maintenance and repairs.
ADJUSTMENT FOR HIGH ALTITUDE LOCATIONS
The steamer has been factory set so that when it is ON and during the READY phase, it will maintain water tem­perature in the steam generator tank at approximately 205° Fahrenheit (just below water boiling point). Howev­er, for high altitude locations, an authorized service agent must adjust the steamer to achieve this temperature. To adjust:
1. Remove side panel and turn control panel power switch to ON.
2. Open compartment door, and after about 15 minutes, steam will be seen, entering the cooking compart­ment.
3. Turn thermostat dial counter clockwise to lower tem­perature until steam just ceases to enter cooking compartment and READY light goes on.
4. Replace side panel.
READY light does not come on after about 15 min­utes,
Water begins to overow into cooking compartment,
Water ll solenoid valve is open, then any or all of
these symptoms may indicate a problem with the operating probe due to either:
1. A short between the operating probe terminal and body of the steamer. Call your authorized service agent.
2. Excessive scale build-up on the operating probe. This acts as an “insulation” and prevents the probe from sensing the water level. It is therefore unable
to close the water ll (solenoid) valve to shut off the
water.
As a temporary solution, with power OFF, unscrew probes, check visually, and clean or chip off scalant. Re­place probe.
This problem is an indication of severe harmful water con­ditions which should be corrected immediately to avoid damage to the components and ultimate malfunction of the steamer. (See WATER CONDITIONING in this man­ual).
5. Follow TESTING PROCEDURES in this manual.
WATER FLOWS INTO DRAIN DURING SHUTDOWN
When steamer is shut down and cold water is running continuously into the open drain, either or both solenoid valves did not close when steamer was turned off.
1. Disassemble solenoid valve(s) and examine for scale or foreign particles lodged in diaphragm or core tube.
2. Clean valve(s) thoroughly and reassemble, or replace valve(s).
DRAIN WATER TEMPERATURE TOO LOW OR TOO HIGH
Cooling solenoid valves are adjustable with ne adjust­ment screw on the bottom of the valve.
1. Run cooking compartment empty until drain tempera­ture stabilizes.
2. Turn ne adjustment screw on cooling solenoid valve out to decrease drain temperature and in to increase drain temperature.
WATER OVERFLOWS INTO COOKING COMPART­MENT
When steamer is rst turned on for the day, and the fol­lowing conditions occur:
HEATER ELEMENTS DO NOT COME ON
When the steamer is turned ON and heater elements do not activate, and therefore, the READY light does not come on, then the contactors may be burned out. If a considerable amount of “chattering” of contactors has been previously experienced, then the thermostat bulb may be coated with scalant and unable to sense water temperature in the boiler accurately, and therefore unable to control the contactors.
1. Replace contactors.
2. Unscrew operating thermostat bulb, clean off scal­ants and screw thermostat bulb back in.
This problem is an indication of inadequate water quality and is not covered under warranty. Have water quality analysed and corrected immediately to avoid complete malfunction of the steamer.
UNIT SHUTS DOWN WHILE IN OPERATION
Pressure switch has been activated due to 5 PSI (35 kg/ cm2) pressure in the generator tank. Pressure in the generator tank is caused due to plugged steam jet tubes or steam diverters due to scale or poor water conditions. Steam jet tubes/steam diverter will have to be cleaned or replaced.
WIRING DIAGRAMS
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