The 0.02uF 600V cap sets the AC signal frequency (5kHz nominal, but is 7kHz on
my TT-1), and every 20% change in value will change the frequency about 10%. The
0.1uF cap to the meter will affect calibration somewhat. Small shifts in frequency
and meter response are compensated in calibration, however, so +/-25% is still
plenty accurate for replacing these two components.
• Disconnected the AC capacitor. This AC cap is used as a series element to set
the 300, 450 and 600mA filament supplies, and this relies on a high tolerance
(better than 5%). Not only did the AC cap in my unit triple in value with age
(which would have accordingly tripled intended filament current), but it started to
heat up and bulge in minutes when loaded! Since I see few circuits with current
driven tube filaments, however, running them from an appropriate voltage instead
should be sufficient. If the AC cap must be replaced, the best choice is probably
polystyrene film types which are AC rated for 150 VAC or more (non AC rated caps
may overheat and do ugly things!). These can also be paralleled to yield exact
values, but such caps are not particularly cheap or compact.
• Replaced out of spec carbon resistors. Carbon resistors tend to change over
time toward the high side. Fortunately most are electrically open on at least one
end and can be checked in situ with an ohm-meter. Any resistor found outside its
tolerance (most are 10%) can be replaced with a new resistor of equal power
dissipation rating (metal film types if possible). Be aware that carbon resistors
that initially check fine may increase their value significantly after being heated,
such as when an adjacent component is soldered, so recheck any old resistors
you leave in after you’ve changed parts! Happily, I found that the precision
resistors on my TT-1 were still within their 1% tolerance.
• Replaced diodes. The original CR-101 silicon rectifiers are not very rugged, and I
found a couple of bad ones. Modern 1N4007 diodes are cheap and superior. I
just clipped one end of the original diode away and bridged the leads with the
new part (Note: the red end of the old diode is the cathode!) For purists who
want to leave the old diodes in, a good CR-101 measures about 0.45V with 1mA
forward current (same as typical silicon diodes).
• Cleaned all contacts. Contacts get covered with oxides and gunk over the years.
I sprayed switches and inside potentiometers with contact cleaner, then rotated
them over the full range a few times. An ohmmeter placed between one end of a
pot and the centre wiper terminal will show smoothly changing resistance as the
control is turned if the pot is clean (this is where a needle type meter is great) and
jump around in value if not. Most pots have a strip of carbon inside and shouldn’t
be treated too roughly, but rheostat windings (such as on the LINE SET and
METER pots) can be scrubbed with a Q-Tip and contact cleaner (I removed the
back plate off of the METER control to clean it as well). The slide switches on my
unit were stiff and balky at first, but a few sprays of flux cleaner and contact
cleaner inside, applied over a few days along with some periodic actuation, got
these working very smoothly (mechanically and electrically). Where convenient,
switch contacts should be checked for a very low contact resistance that doesn’t
change when the switch is wiggled sideways. Tube socket contacts were cleaned
with a pipe cleaner (something a bit tougher would have been nice) and contact
cleaner. Any switch or control that remains intermittent after a while should be
replaced, as these can damage a tube under test with transient conditions.
• Replaced tube sockets. In my case, the miniature 7 and 9 pin sockets were worn
to the point of loose, intermittent contact during test. I could not readily find a
replacement for the 9 pin socket, so I replaced the contacts with those removed