GE P&W FuelSolv User Manual

Page 1
Find a contact near you by visiting www.ge.com/water and clicking on “Contact Us”.
* Trademark of General Electric Company; may be registered in one or more countries.
©2011, General Electric Company. All rights reserved.
TP1189EN.doc Jun-11
Paper
Slag Control Treatment Program at a Southeastern Utility
Authors:
M. Domingo Tubio, Product Applications Engineer
Rick Higginbotham, Account Executive
Abstract
Coal-fired power plants supply over half the electric­ity to the US grid. Currently, utilities are facing a range of challenges including decreasing industrial demand for electricity, competition from low cost natural gas and rising coal prices. High quality East­ern bituminous Central Appalachian (CAPP) coal costs are increasing due to rising exports, increasing transportation and environmental costs and de­creasing production, (Buchsbaum 2008; Metzroth
2008). To stay competitive, some utilities are investi­gating burning lower-cost, lower-quality “opportunty” coals such as Northern Appalachian (NAPP) and Illinois Basin. The most efficient plants can be dis­patched for longer periods for improved financial performance. The change to lower rank coal and increased operation can result in increased slag de­posits in the furnace and superheater areas, (Gabriel
2011).
A Southeastern utility desired to blend lower-cost low ash fusion temperature Northern Appalachian (NAPP) coal with their typical CAPP coal in their 745 MW pulverized-coal boiler. Sootblower cleaning alone is not effective when slag deposits are a liquid or pseudo-plastic state which deforms under pres­sure. A proprietary mixture of chemical additives was recommended to elevate ash fusion tempera­ture and modify the deposit to make it more easily removable by sootblowers. The blend is a unique combination of water-soluble magnesium hydroxide and copper oxide slurries which has a synergistic effect when used together to mitigate slag for-
mation and impact. During the fourth quarter of 2010, the utility consumed over 44,000 tons of NAPP opportunity coal treated with this combina­tion of proprietary fireside chemical additives over
a four week period. GE’s approach allowed the
customer to minimize the detrimental effects of burning slag prone coal while reducing fuel costs. This paper summarizes the trial and performance results.
Slag and Fouling Formation and Cost
There are numerous non-combustible inorganic impurities in coal besides hydrocarbons. Depend­ing on the ratio of these minerals and compounds, slagging and convective pass fouling can occur in boilers. Slag formation accelerates when the fur­nace exit gas temperature (FEGT) exceeds the fu­sion temperature of the ash. Indices such as the basicity ratio can help predict slag viscosity and ash fusion temperature (Babcock & Wilcox 1978).
As slag density increases with time and tempera­ture, a deposit is formed that is difficult to remove
with sootblowing. Deposits can “grow” as particles
accumulate; it is not uncommon to observe large deposits on the leading edge of platen superheat tubes and secondary superheater tubes above the bull nose of the boiler. When the slag eventually falls it can damage tube banks lower in the boiler, resulting in unscheduled outages and lower avail­ability.
CAPP coal typically has a high ash fusion tem­perature and less tendency to create excessive slagging. NAPP coal is becoming more economi­cally attractive for several reasons, including availability at lower delivered costs than CAPP coal (Pusateri 2009). Figure 1 illustrates the chal­lenge of using NAPP coal with a lower ash fusion
Page 2
Figure 1: Fuel Comparison and Basicity Ratio (Babcock & Wilcox, 1978)
temperature. Slag deposits are expected to be in
Fuel Type
Typical
Opportunity
** Basicity Ratio = (Fe2O3+CaO+MgO+Na2O+K2O)
(SiO2+Al2O3+TiO2)
Source
Central
Appalachian
Northern
Appalachian
Cost per ton, $US (2010)
$70 – $75
$58 – $70
HHV, Btu/lb
~12,000
~13,000
SO2, lb/MMBtu
1.1 – 1.5
4.5 – 5.0
Ash, wt%
11 – 12
7 – 8
Moisture, wt%
6.7 – 7.0
6.0 – 7.0
Ash Soften­ing Temp, deg F
2,700
2,250 Basicity Ratio **
0.12 – 0.14
0.45 – 0.55
Ash, wt%
SiO2
Al2O3
Fe2O
3
K2O
TiO2
MgO
CaO
Na2O
53 – 56
28 – 30
5 – 6
3.3 – 3.6
1.3 – 1.5
0.9 – 1.0
0.7 – 1.3
0.2 – 0.3
39 – 40
20 – 21
22 – 24
1.3 – 1.4
0.85 – 0.95
1.05 – 1.15
5 – 6
0.95 – 1.05
liquid state at furnace temperatures with noncom­bustible mineral content present. Sootblower clean­ing alone is not effective when the slag is a liquid or pseudo-plastic state which deforms under pressure.
Fouling, which is closely related to slagging, usually occurs in the boiler’s cooler convective back-pass section as gaseous ash components (such as sodi­um and potassium) condense. It typically occurs in the vertical and horizontal reheaters and primary
superheater. Fouling deposits can “bridge” across
tubes and restrict gas flow.
That increases induced fan horsepower, which raises the plant heat rate and, therefore, lowers plant efficiency. Slagging and fouling can result in derating (shedding load) and costly unscheduled outages and repairs from damaging slag falls. But these problems can be eased by combining chem­ical additives for fireside applications with me­chanical removal (sootblowers).
Boiler and Trial Design
The 745-MW pulverized coal-fired boiler is a Riley Stoker Corporation front-wall fired boiler with 2,500,000 lbs/hr steam production at 2610 psig and 1,005 deg F at superheater terminal outlet.
Page 2 Technical Paper
Page 3
Figure 2: Trial Trailer and totes of additives (left) and applying product to NAPP coal (right)
The boiler fires 250 tons pulverized coal per hour at maximum load, and the boiler train is equipped with SCR, cold-side electrostatic precipitators and a wet flue gas desulfurization (Wet FGD) scrubber system.
Trial results using the same opportunity fuel- NAPP coal- at a sister station indicated it could not be burned untreated, as the resulting slag was severe enough to slag the boiler and block the gas path. Operating experience indicated boiler conditions could deteriorate within days of introducing oppor­tunity fuel. To minimize the risks of boiler outage during trial, the utility blended its typical fuel with a small proportion of opportunity fuel treated with a mix of proprietary chemical additives to reduce se­verity of fireside slagging. Product dosages were optimized as the percentage of opportunity coal was increased until it reached the target level of 50 percent.
Chemical Additives for Slag Control
A range of chemical additives were considered be­fore the two products were selected based on ulti­mate analyses of the fuels. The proprietary mix of additives selected for this trial included a magnesi­um based compound and a metal oxide. The mag­nesium is known in the industry to elevate ash fusion temperatures due to the high melting point of magnesium oxide. This treatment keeps the slag in a solid state instead of liquid-phase deposit. The metal oxide-based slurry contains copper which has been used in the industry as a combustion catalyst. Less well known is that copper can reduce the co­hesive strength of the ash via a nucleating effect with iron species. Gradual thermal decomposition of the metal oxide product also makes the slag porous and, therefore, weaker. These mechanisms com­plement the magnesium effect for certain types of coals or coal blends, depending on the ratio of min­erals and other non-combustible species. Together,
the proprietary additives create fracture planes in the solidified slag, weakening the deposits so that they can be more easily removed by sootblowers.
Treatment Application
The chemical additives were transferred from agi­tated trailer-mounted base totes to the coal belts via peristaltic pumps, where the chemicals were the dosed at predetermined amounts via a mani­fold mounted above the coal conveyor (Figure 2).
Dosing occurred when the coal belts conveyed NAPP coal. Aqueous magnesium-based slurry dosages were reduced from 3 lbs of product per ton of NAPP coal to optimum of 1.0-1.5 lbs. Aque­ous metal oxide slurry was introduced to deter­mine its impact on slag mitigation in conjunction with the magnesium-based product. It was de­termined that the optimum product feed rate was
0.25 lbs product per ton of NAPP coal. The NAPP coal quantity was ramped up from 16 percent to the target of 50 percent, where it was maintained for a week until the end of the trial. The dynamic test environment confronted the trial team with challenges that included outages, inclement weather, and real time adjustments to the dosage based on visual observations of furnace slag con­ditions.
Trial Details
To be considered successful, the trial had to meet several criteria, including:
1. Demonstrating that the magnesium content
increases the ash fusion temperature and, therefore, makes the deposit more friable and easily removable.
2. Demonstrating the metal oxide slurry syner-
gistically assists in slag mitigation.
Technical Paper Page 3
Page 4
3. Determining the optimum product feed rates for
the CAPP/NAPP blends while monitoring (with an infrared (IR) camera) real-time slagging phe­nomena along with boiler parameters such as load, pressure drop, and exit temperature. Cus­tomer’s fuel blends included 84 percent CAPP/16 percent NAPP, 77 percent CAPP/33 percent NAPP, and 50 percent CAPP/50 percent NAPP as
the “highest stress test.” (the untreated “base- line” NAPP blend slag indices were not available,
as they presented unacceptably high operation­al risks to the customer.)
Mid-December- following a number of
weather-related outages, inclement weather compelled the suspension of the trial.
After a weather-related equipment out-
age, NAPP coal treatment was resumed. Dosage was increased by 10 percent after
a “gooey slag” was seen in the furnace.
The slag subsequently returned to its semi-solid state.
December 20- the trial concluded.
4. Demonstrating that the use of magnesium
and/or metal oxide products has no adverse ef­fects on boiler operations- i.e., it does not exac­erbate slagging or fouling or emissions. Obtained Flue Gas Desulfurization (FGD) wastewater grab samples and ash pond sam­ples, analyzed for copper and other compo­nents.
Data was recorded during the “baseline” (100%
CAPP coal) and chemical treatment trial periods, as­suming equipment parameters such as tube clean­liness, sootblower availability, and thermocouple calibrations. Note that during the chemical trial the unit was not derated overnight for deslagging. Overnight load shedding allows the slag to contract in the cooler flue gas, and this uneven contraction in the matrix causes cracks and gravity-assisted re­moval of the accumulated slag. This beneficial pro­cedure was not conducted during most of the chemical trial (Figure 3).
Here is the key chronology of the trial
November 15- the chemical trial began as
16 percent NAPP coal was dosed at 3.0 lbs/ton magnesium-based product on the coal belt en route to bunkering silos #5 and #6.
DCS Data
The trial team collected data every 5 minutes from
the customer’s “Pi” distributed control system
(DCS), including load (MW), heat rate (MMBtu/hr), furnace exit gas temperature (FEGT, deg F), soot­blower, and coal mill operation including feeder flow (kpph). For the analysis, the team removed all data points below 700 MW so that only “full load” data was considered and outliers could not im­pact calculations.
The most obvious change over time was soot­blower activity. If at least one of the 60 IR (radiant) or IK (convective) sootblowers was active when the data was recorded, the event was logged in Pi. In the DCS, sootblowers were either “on” or “off”; it was not possible to record which sootblowers were active. The trial team decided to record the average number of sootblowers per day to under­stand how this rate was changing over time. The frequency seemed to have doubled as the NAPP was increased from 0 (baseline) to 33 percent and apparently tripled by the time the trial achieved 50 percent NAPP. It is important for a utility to keep this parameter in mind given operations concerns such as steam consumption and tube wear over time.
November 24-29- the trial was suspended
over Thanksgiving
December 1 and 2- duct testing occurred.
The flue gas sampling successfully obtained a baseline for the CAPP/NAPP blend while the treatment consisted only of magnesium­based product. The magnesium-based product dosage was decreased as the metal oxide product was introduced.
Page 4 Technical Paper
Furnace Exit Gas Temperature (FEGT) data is valu­able for a slagging study since it can be a proxy indictor of slag conditions. FEGT values should rise as slag increases, since slag is an excellent insula­tor and because increasing slag conditions will push the fireball farther back into the convective pass of the furnace, this analysis indicated that furnace operation vis-à-vis FEGT was approxi­mately equivalent during the baseline and chemi­cal treatment periods. The team observed decreasing temperature variances between east and west side thermocouples across the boiler.
Page 5
Figure 3: Key Dates of Trial and Results Summary (for Gross Load >700 MW)
The data below (Figure 3) presents average parame-
PARAMETERS
(start – end dates)
10/18 – 11/14
11/15 – 11/23
11/30 – 12/3
12/4 – 12/8
12/10 – 12/12
12/17
12/18 – 12/20
NAPP Coal, %
0
16
33
33
50
50
50
Magnesium product, lbs/ton
0
3.0
2.0
1.5
1.5
1.0
1.1
Metal oxide product, lbs/ton
0 0 0
0.25
0.25
0.25
0.275
# of Pi data points
4,118
342
634
391
699
123
771
Avg # of sootblows/day
36
57
63
82
104
94
157
Avg Heat Input, MMBtu/hr
7,003
7,060
6,278
6,216
6,892
6,953
6,986
Avg Coal to Boiler, ton/hr
336
321
325
327
327
332
331
U3A Avg Max FEGT, oF
2,318
2,683
2,602
2,496
2,468
2,561
2,627
U3B Avg Max FEGT, oF
2,497
2,536
2,464
2,486
2,521
2,479
2,511
ter values from the trial, implies that chemical treatment does not adversely impact the boiler. A longer trial could indicate if boiler operation signifi­cantly improvers with chemical treatment while burning the opportunity coal.
Infrared Photography
The camera’s integral flame filter and high tem­perature range covered the boiler’s operating range throughout the trial and its multi-spot tem­perature measurement capability enabled final images to include reference temperature profiles, (Mikron 2011). Thermal photos of the boiler slag conditions were recorded at the boiler ports throughout the trial.
The trial team used port inspection and photog­raphy to monitor boiler slagging conditions in the furnace. The team developed a standardized nam­ing convention for referencing boiler ports at vari-
ous elevations. For example, port “3A4E” refers to
Unit 3, Alpha side, Level 4, Port E. This ensured that slagging conditions were properly recorded, since more than a dozen trial team members viewed, photographed, and commented on the visual condi­tions during the trial.
Visual and infrared (IR) photos of conditions at the various boiler elevation ports (Figure 4) were made with an Olympus brand “point-and-click” digital camera and a Mikron Lumasense brand infrared camera.
Slag conditions inside the boiler were recorded with a portable, battery-operated Lumasense Mikron­brand model 7604F infrared camera.
Not only were visual observations of these condi­tions important, they were, arguably, the best way to measure the impact of chemical treatment on boiler slag, since instantaneous changes in many variables (such as sootblower activity, number of pulverizers in operation, load changes, etc.) make it difficult to compare with other parameters in isolation (such as FEGT).
Several photos of the slagging conditions in the boiler on November 23 and 30 (Figures 5 and 6) clearly show the bottom of the superheater (SH) pendant and no or minimal slag accumulation. There was some initial concern about the under­side of the tubes at Level 3; however, the slag was removed with a firm push of a spade. Overall slagging was considered minor at this point, and noticeably worsened as the inspection continued down the boiler. (The worst slag was near the burners.)
Technical Paper Page 5
Page 6
Figure 4: Unit 3 Ports (Elevation Drawing #69085B5, revised 2-19-99)
Plant monitoring and the attached pictures from the
Port Name
Port Qty
Elevation
Notes
Level 1
Ports A,B
2
~580’
Pendant Superheater
Level 2
Ports A,B,C,D
4
~566’
Cold Reheat Piping
Level 2.5
Port A
1
~563’
Above bullnose
Level 3
Ports A,B
2
~550’
Below bullnose Level 4 Ports
A,B,C,D,E,F
6
~538’
Bullnose
Level 5
Ports A,B,C,D
4
~520’
Wall tubes
Level 6
Ports A,B,C,D
4
~506’
Wall tubes
Level 7
Ports A,B,C,D
4
~496’
Wall tubes
Level 8
Ports A,B
2
~488’
Overfire Air
Level 9
Ports A,B,C,D
4
~483’
Burners
Level 10
Ports A,B
2
~473’
Below burners
early phase of the trial revealed that the slag for­mation was minimal, with little day-to-day change, and was being removed by the sootblowers where possible. Several locations were identified for possi­ble future installations of IK sootblowers to minimize slag formation. Initial indications showed the slag to be self-limiting and still friable. Operations and GE continued to monitor and report on slag formation, and GE continued to photograph the Unit at these ports and report the finding after each inspection.
By December 17, the trial team began burning 50 percent NAPP, dosed with 1.0 lbs. magnesium­based product per ton and 0.25 lbs. metal oxide­based product per ton. Since the slag appeared gooey and there was concern over the sub­minimum amount of feed required for operation, both feeds were increased 10 percent (Figure 6). By December 20, the boiler recovered and slag­ging conditions had improved.
Page 6 Technical Paper
Page 7
3A Level 1 Port A, 11-30-10
3A Level 1 Port A, 11-30-10
3A Level 3 Port B, 11-30-10
3A Level 3 Port C, 11-23-10
3B Level 4 Port E, 11-30-10
3A Level 4 Port A, 11-23-10
Figure 5: Visual and IR Photography, 11-23 and 11-30
Technical Paper Page 7
Page 8
Figure 6: Visual and IR Photography, contrasting 11-30-10 with 12-17-10
Wastewater and Ash Pond Analyses
3A Level 5 Port D, 11-30-10
(note the minor slag)
3A Level 5 Port D, 12-17-10
(note the large formation on the wall)
3A Level 3 Port B, 11-30-10
(note the minor blinding)
3A Level 3 Port A, 12-17-10
(note the blinding and hot runny formation)
SO3 Testing
Two FGD water discharge samples were collected in order to establish a baseline. No measureable cop­per was detected and no significant change in op­eration was noted. In future trials, additional samples should be taken to provide a greater un­derstanding of the normal state of the FGD compo­site analysis.
Ash pond water samples were collected on Novem­ber 19 and 20 (prior to the metal oxide addition) and on December 12 (after the metal oxide feed) to de­termine the effects of copper in the ash pond. The trial team wanted to rule out any negative impacts from copper carryover from the bottom ash sluice into the ash pond and subsequent NPDES outfall. No measurable copper was detected in the ash pond on all three sample dates.
The trial team also conducted two duct tests, sampling flue gas to determine the sulfur trioxide (SO3) concentration during varying operating con­ditions and when chemicals were added to the coal feed. Samples were collected from a single point approximately seven feet from the duct wall at a test port downstream of the SCR- the only test port available at the furnace. Measurements were conducted to observe the treatment regi-
men’s effect on “blue plume”. (There have been studies on magnesium oxide’s effect on SO3 in
fossil fuel-fired furnaces (Schmidtchen 2002)). Ammonia injection was off during the testing to avoid free ammonia interference with the analy­sis. A third-party stack testing firm was contracted to collect samples using the Controlled Conden­sate Method (US EPA Method 8A) and analyze them by High Performance Liquid Chromatog­raphy (HPLC).
Page 8 Technical Paper
Page 9
The untreated opportunity fuel SO3 baseline was
Run No.
Sample Time (EST)
SO3 Concentration (ppm, dry basis)
Start
End
11/30 and 12/1 – 33% NAPP Coal, 2.0 lb/ton magnesium-based product
1
10:40
11:40
11.3
2
13:05
13:50
12.3
3
14:45
15:30
13.0
4 *
16:25
17:10
6.0 *
5
08:37
09:22
12.4
6
12:10
12:55
9.5
7
14:05
14:50
11.6
8
16:05
16:50
15.3
Average
12.2
12/11 – 50% NAPP Coal, 1.5 lb/ton magnesium-based product
and 0.25 lb/ton metal oxide-based product
9
08:30
09:15
13.6
10
10:05
10:50
12.1
11
11:30
12:15
9.5
12
12:45
13:30
10.4
Average
11.4
Run 4 is suspected as an outlier when compared to other runs under the same operating condition and is not included in the calculated average.
Figure 7: SO3 Testing Summary
unavailable, and the SCR is expected to convert some SO2 to SO3. The testing indicated that the ap­parent SO3 removal was within sampling error and that there was no observable difference in the SO3 mitigation when MgO addition rates were varied. Thus, the results did not indicate that the MgO chemical treatment significantly mitigated SO3 in the furnace. However, it is also important to note that there was no apparent increase in SO3 for­mation overall on December 11, when the copper­based metal oxide slurry was added to the system (Figure 7).
Trial Results and Conclusions
The magnesium-based product alone showed an improvement in slag removal until the NAPP blend increased above 33%. Magnesium alone could not elevate ash fusion temperature to avoid sticky deposits in the upper regions of the furnace, Te­nacious, viscous deposits throughout the boiler became firmer and were easily removed by IR and IK sootblowers during the trial once the magnesi­um and metal oxide products were combined.
Technical Paper Page 9
Page 10
The visual observations and operator feedback indi­cated that the synergistic combination of the 1.0-lb to 1.5-lb magnesium-based product range per ton of NAPP coal in conjunction with 0.25-lb metal ox­ide-based product per ton of NAPP coal was very effective in mitigating slag of the blended fuel. Dif­ferent coals or coal blends may require customized product ratios to appropriately address potential slagging issues.
In addition, several locations were identified as pos­sible sites for future IK sootblowers and observation ports to control and monitor slag formation. Lessons learned include the importance of freeze protection on the lines and providing options for continuous mixing with water-based slurries to reduce material handling difficulties. Future trial goals include quan­tifying loss on ignition (LOI) with the metal oxide slur­ry and evaluation of different additives for SO3 control in the furnace.
Estimates for fuel cost savings are projected to range from $5,000,000 to $13,000,000 per year by switching to a 50 percent blend of NAPP opportunity coal. Even greater savings could be achieved by in­creasing the blend to include Southern Illinois Basin (ILB) coal, (Figure 8).
References
Babcock & Wilcox. “Steam”. 39
1978.
Buchsbaum, Lee. “New Coal Economics”. En-
ergybiz, November / December 2008. Retrieved from
http://energycentral.fileburst.com/EnergyBizO nline/2008-6-nov­dec/Financial_Front_New_Coal.pdf
Gabriel, Mark, Manager of Business Develop-
ment, GE Water & Process Technologies. “Slag Control Treatment Program at EKPC Spurlock Station.” Presented at Electric Power Confer­ence, Chicago, IL. May 2011.
Hatt, Rod. “Correlating the Slagging of a Utility
Boiler with Coal Characteristics”.
Retrieved from
http://www.coalcombustion.com/PDF%20Files /CorreSlagefc03.pdf April 2011
Metzroth, Lawrence, VP Analysis & Strategy,
Arch Coal Inc. “Regulatory and Other Con- straints on CAPP Coal Supply.” Presented at
7th Annual Coal Trading Conference, New York City, NY. December 2008. Retrieved from
http://www.coaltrade.org/wp­content/uploads/2011/02/Metzroth.pdf
th
Edition,
Mikron camera information retrieved April
2011 from
http://www.mikroninfrared.com/EN/products/t hermal-imagers-detectors-and­cores/portable-thermal-imagers/portable­special/m7604f.html
Pusateri, Robert, President Consol Energy
Sales. “NAPP and the Marketplace.” Present­ed at McCloskey Coal USA 2009 Conference, New York City, NY. June 2009. Retrieved from
http://www.consolenergy.com/Newsroom/Spe
Figure 8: Customer’s Coal Price Ranges
eches/McCloskeyNewYork2009.pdf
Schmidtchen, Paul. “High Activity Magnesia
Use for SCR Related SO3 Problems.” Presented at NETL 2002 Conference. Retrieved from
http://www.netl.doe.gov/publications/proceed ings/02/scr-sncr/schmidtchensummary.pdf
Page 10 Technical Paper
Loading...